Saga with my 87 Chevy Truck continues
Posted: Sun Jun 26, 2016 10:08 pm
With unknown origins of some of the parts used in the previous owner's 134a conversion and issues I was having the last time I tried to charge it, I tore everything apart, flushed it all again, new blue orifice tube, new receiver/dryer(accumulator), and brand new H6 compressor. All lines also got new orings. When I flushed this time, everything was clean (even when I flushed the last time, I really didn't get any dirt, just a lot of old oil in the evap). Got it all back together today and started charging it. Ambient was about 105 and it was humid. Compressor called for PAG 46, but none of the local shops had any, and the compressor mfg stated that PAG 100 could be also used. Put 5oz PAG 100 in the receiver/dryer, and the compressor came pre-filled with 3oz PAG 46. Pulled vacuum for 30 min. Let it sit for 30 min and it held the vacuum. Started pumping in R134a. System originally called for 3.25lbs of R12, so I was targeting 42oz of 134a (52 x .80 = 42). While I was on the 3rd can, my low side pressures were already in the high 40's and the high side pressure was nearing 300. Vehicle also has a brand new heavy duty fan clutch and it is moving noticeably more air than the old one, plus I also had a fan blowing directly into the condenser. When the pressure hit about 300, the compressor seized and the clutch began to slip. I immediately shut off the A/C. At that point, I hit the condenser with some water and the pressure dropped down below 200. I started it back up and the pressure stayed low and it started taking a charge again. When the pressures would get up near 300, I would wet the condenser and could get the pressure under 200. I continued this until I got it charged, and ended up with about 44oz in. Vent temps never got better than 75 degrees. At that point, I needed to shut down for a while. Later in the evening, I fired it up and within about 2 seconds the compressor froze and the clutch slipped. Working the switch on and off, I was able to finally get the compressor to run, but vent temps were in the high 70's. I didn't have the gauges on it at the time so I don't know what my pressures were.
I don't get why the high side pressures were so high. There was a lot of air flow through the condenser - you can really feel and hear the fan working. Even when I hit it with water, I didn't get a reduction in vent temps. Something I did notice when I was flushing is that the condenser seemed to have a restriction - there wasn't as high of an air flow going through it as there was through the evap.
Any ideas? Anything I should look at or check?
Side note - when installing conversion fittings on the ports, should I have pulled out the schrader valves from the old ports?
Thanks!
I don't get why the high side pressures were so high. There was a lot of air flow through the condenser - you can really feel and hear the fan working. Even when I hit it with water, I didn't get a reduction in vent temps. Something I did notice when I was flushing is that the condenser seemed to have a restriction - there wasn't as high of an air flow going through it as there was through the evap.
Any ideas? Anything I should look at or check?
Side note - when installing conversion fittings on the ports, should I have pulled out the schrader valves from the old ports?
Thanks!